Friday, April 17, 2015

Post #28

What we accomplished:
  • Robot went around the chair once
  • Fixed the motor on the robot
This week we managed to take one part of our robot apart to tighten some screws that were loose. We also added new screws to places that needed it. We continued to work on the coding to try and get our robot to go around a second time. However, we haven't been too successful with our attempt. Hopefully next week we can get it to go around twice if not three times around the two chairs.


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